tlkenyon
Well-known member
- Joined
- Sep 30, 2010
- Messages
- 679
- Fluid Motion Model
- R-25 SC
- Non-Fluid Motion Model
- 3 kayaks, 1 canoe; R-21 (Nellie May I)
- Vessel Name
- Nellie May
- MMSI Number
- 338219131
Yesterday, I had a mechanic replace the impeller, and while he was on the boat (2015 25sc) check and then replace the shaft packing. We are in Orillia, Ontario in the Mideast of doing the Great Loop and now have just short of 1,000 hours on the boat. Original impeller and shaft packing. Have previously adjusted the packing several time and thought it might be time for replacement.
Underway after the work, I shot the packing nut with my laser thermometer and saw 120F, when at 1600 rpm. After ramping up to WOT (2850 loaded like we are), measured 140F which shortly climbed to 165F. Backed down and made it to a marina. Was seeing 1-2 drips every 5 seconds or so.
Next morning, after she cooled off, backed the packing nut off about one-quarter turn (about 2 flats on the nut). When retightening the Lock nut, it pushed the packing nut off the end of the shaft log. Try as I might, I could not get the packing nut to engage the threads on the shaft log. Needless to say, water was coming in....but bilge pump is keeping up.
I think the mech put in too many rounds of packing or did not get all the old packing out. It came out in pieces, so was hard to tell.
Waiting right now for him ( who shall remain nameless for now) to return to the boat to remedy the situation.
Anybody got any wisdom for me?
Will update later.
TK
Underway after the work, I shot the packing nut with my laser thermometer and saw 120F, when at 1600 rpm. After ramping up to WOT (2850 loaded like we are), measured 140F which shortly climbed to 165F. Backed down and made it to a marina. Was seeing 1-2 drips every 5 seconds or so.
Next morning, after she cooled off, backed the packing nut off about one-quarter turn (about 2 flats on the nut). When retightening the Lock nut, it pushed the packing nut off the end of the shaft log. Try as I might, I could not get the packing nut to engage the threads on the shaft log. Needless to say, water was coming in....but bilge pump is keeping up.
I think the mech put in too many rounds of packing or did not get all the old packing out. It came out in pieces, so was hard to tell.
Waiting right now for him ( who shall remain nameless for now) to return to the boat to remedy the situation.
Anybody got any wisdom for me?
Will update later.
TK