jkhiser
Well-known member
- Joined
- Feb 16, 2018
- Messages
- 54
- Fluid Motion Model
- R-21 EC
- Hull Identification Number
- FMLC2831A313
- Vessel Name
- Wenniway
- MMSI Number
- 338165185
Replacement of shaft packing on Cutwater 28.
Packing replacement was due. Colleen at Diversified Marine did the work, with some assistance calls to Fluid Motion. I did not capture who helped her with information from the factory.

There was not sufficient clearance to get packing removed and installed due to the length of the stuffing box hose. There was also not sufficient clearance to access the shaft coupling nut to allow removing the shaft.

The stuffing box hose was split, allowing insertion of a cut down wrench to free the coupling nut. Coupling was rebolted to the tranny, then shaft removed with shaft hammer.


Stuffing box and shaft coupling were cleaned up in the shop.



On reinstall, the shaft tube was undersized. Caulking had been used to build up to diameter of the stuffing box hose. All old caulk was ground off, and a short section of hose was used as mold for new thickened epoxy. This was faired out.



All reassembled with new packing, new hose, clamps, and shaft key

The new hose was cut shorter to allow simpler packing replacement in the future.

Shaft alignment will be completed once launched.
Whether or not the packing replacement was “due,” it was time to get all the corrosion cleaned up before, among other problems, the coupling nut became permanently frozen.
Pictures at: gallery2.php?g2_itemId=71190
Packing replacement was due. Colleen at Diversified Marine did the work, with some assistance calls to Fluid Motion. I did not capture who helped her with information from the factory.
There was not sufficient clearance to get packing removed and installed due to the length of the stuffing box hose. There was also not sufficient clearance to access the shaft coupling nut to allow removing the shaft.
The stuffing box hose was split, allowing insertion of a cut down wrench to free the coupling nut. Coupling was rebolted to the tranny, then shaft removed with shaft hammer.
Stuffing box and shaft coupling were cleaned up in the shop.
On reinstall, the shaft tube was undersized. Caulking had been used to build up to diameter of the stuffing box hose. All old caulk was ground off, and a short section of hose was used as mold for new thickened epoxy. This was faired out.
All reassembled with new packing, new hose, clamps, and shaft key
The new hose was cut shorter to allow simpler packing replacement in the future.
Shaft alignment will be completed once launched.
Whether or not the packing replacement was “due,” it was time to get all the corrosion cleaned up before, among other problems, the coupling nut became permanently frozen.
Pictures at: gallery2.php?g2_itemId=71190