A successful day with the boat out of the water. Thanks for all the suggestions. It was pressure washed and I was happy with how little growth was on it. A few barnacles on unpainted metallic surfaces. I used the hose picks as suggested to clean the through hull intakes, behind the screens. Worked great.
I replaced the anodes, they were all but gone.
I replaced the broken trim tab actuator. Which worked out pretty well, not too hard once I got the hydraulic line off.
I replaced the trim tabs with drop fin trim tabs. Once I had it all put back together, it worked once on testing and then the new actuator stopped working. As it turns out, the toggle switch for that side had broken (what are the chances of a switch failure right in the middle of repairing a downstream component, the actuator). Easy to replace the switch and all worked well.
I did most of what you all suggested, minus removing the main prop and greasing the rudder shaft.
Put her in the water and went out to test the new drop fins. Not working while at speed underway. Worked fine at the dock, but not underway........hmmmm
My engine hatch lift had not been working either since the trim tab actuator failure earlier in the summer. So I thought there may be a relationship between the two issues since they run on the shared hydraulic power unit.
So today I decided to detatch the hydraulic line from the engine hatch lift and wanted to see if I was getting pressure at the end of the line. I ran the pump via the engine hatch switch and found the problem.........
instead of automatic transmission fluid, a little pink foam came out followed by water.
It turns out, when the trim tab actuator broke and I continued to try to use it, the system pulled in water, likely through the broken actuator. So I drained (via the detached engine hatch hydraulic line) all the foamy, watery fluid, filled it partially with new ATF, ran the trim tabs up and down multiple times, drained again and repeated until just ATF was coming through.
Went out to test the new drop fins and all worked great. I now have plenty of trim power and gained speed and about 100-200 rpm WOT. It was a short test and I will try it out more completely soon to get some real numbers.
The engine hatch is still not working, but I did not try to troubleshoot any further. I am considering just leaving it unattached and manually raising and lowering, propping open with a piece of wood. Even when it was working, it was slow and sometime would get stuck open and not lower (maybe the solenoid at the HPU). Interestingly enough, the only times it would get stuck open was when detached from shore power. When plugged in to shore power, it would lower again.
All in all I made great progress.....and still have some projects to finish.