What did you work on/fix today?

After 10 years finally fixed engine coolant flow to water heater. It has always taken about two hours running at least 1500 rpm to get good hot water. We've worked around it by always showering on days that we travel. Finally installed a $20 booster pump and short circuited the fwd heater(which we don't use).

As with anything on the 25 Classic it was a real pita to get to things. Mounted the pump right beside the shower sump pump which is just fwd of the water heater. Used the circuit for the long since removed maserator pump for power. Now even at idle we get hot water in under an hour.
 
Finally got around to putting more fans in the main area. Lack of airflow on florida days is miserable when i dont want to run the AC. Figured i would put a pair of Sirocco fans in.
Shockingly, it was a 15 minute project.
I used the windshield wiper wiring (there is a switched, constant and ground right there) with a couple wago splices and they are good to go. They use almost no power and wont impact that circuit at all.
Untitled by Grant Wilson, on Flickr
Untitled by Grant Wilson, on Flickr
Untitled by Grant Wilson, on Flickr
Fully adjustable in all directions and also can swing up out of the way if you dont want to see them. Absolutely love these things
 
Lewmar ProFish 1000 repair.
In 2020 we replaced the windlass on our 2009 model R25. Had replaced the windlass motor(seized up) in 2016 and new that a complete overhaul would be needed this time so elected to replace the windlass completely. At time of the motor repair the windlass had a lot of water in it as is typically reported when people open them up. The new windlass installed in 2020 was a "gen 3" model with improved gasket on the split line. The windlass locked up while deploying the anchor on our first trip of this season. I was really disappointed that we only got five years of life out of it. Based on the symptoms and on my previous experience I assumed it was another motor failure. However when I opened it up the internals were in pristine condition with no moisture at all inside and no signs there had been any. And the motor was fine. So apparently the casing gasket in the gen 3 model is effective.

To make a long story short(ish) what failed this time was that the retaining nut on the compound gear(part no.51) came loose and backed off. The threads on nut and shaft were damaged. I was able to clean up the threads on the shaft but not on the nut. It's a specialized nut and is not sold separately by Lewmar. It comes as part of the compound gear assembly which is $140 item. I wasn't able to locate a replacement nut either on line or at local industrial fastener suppliers. So I ended up buying a standard hex nut for under a dollar and modified it on a bench grinder(pic below). Happy to say the modified nut worked and the windlass is back in service.

Good news is that the re-designed gasket on the gen 3 model of this windlass is effective. So Lewmar has corrected the biggest complaint/source of failure on this model windlass.

Compound gear assembly. Note retaining nut on end of shaft in left side of pic below.
View attachment 25623

Pic below: original retaining nut on left, modified piece in middle, standard hex nut on right.

View attachment 25621
 
Thanks for this info. My motor seems to run when I hit the up and down buttons (I hear a whirring sound) but the gears are not turning. Do you think this retaining nut is a good place to start? The gears all look like they are in good shape. Any other ideas as to why the unit isn’t functioning?
 
Android GX Wifi Display
Victron has a new app that turns any Android device into a dedicated GX display. I took and old 9" android and installed the app which turns it into a dedicated GX display. Works great. Installed in front of the wiper motor assembly. Instant display of solar, DC-DC charger, Inverter and AC & DC loads, much better than the Garmin integration and easy to do. Highly recommend for those who have a CerboGX installedView attachment 25768View attachment 25769
Looks great! love a software solution!


im curious the value you get from the cerbo data. is it just to bring attention to the power usage at any given moment? seems like an expensive piece of kit for that purpose?
 
Thanks for this info. My motor seems to run when I hit the up and down buttons (I hear a whirring sound) but the gears are not turning. Do you think this retaining nut is a good place to start? The gears all look like they are in good shape. Any other ideas as to why the unit isn’t functioning?
What do you mean by the "gears are not turning"? Do you mean the gypsy is not turning? Does it turn in either direction? And you said the gears are in good shape. Does that mean you cracked the casing and took a look?
 
What do you mean by the "gears are not turning"? Do you mean the gypsy is not turning? Does it turn in either direction? And you said the gears are in good shape. Does that mean you cracked the casing and took a look?
Hi Dan, I did crack the casing. I hear a whirring sound of the motor, but generally the gears are not turning and neither is the gypsy. Other than a very greasy gear case, the gears appear not to be stripped. Very rarely, it goes into gear and the gears/Gypsy turns. I’m wondering if there is an issue with the 10mm dowels. I have read this on other posts. Any info would be appreciated.
 
Hi Dan, I did crack the casing. I hear a whirring sound of the motor, but generally the gears are not turning and neither is the gypsy. Other than a very greasy gear case, the gears appear not to be stripped. Very rarely, it goes into gear and the gears/Gypsy turns. I’m wondering if there is an issue with the 10mm dowels. I have read this on other posts. Any info would be appreciated.
There is a pin that drives the gear on the motor shaft. If that fell out or sheered it could do as you describe if there's no load on the gypsy. If I recall how the nut on the pinion comes into play the gears should still spin in the deploy direction but not in the retrieve direction. If you're referring to the dowels under the gypsy they wouldn't have any effect on whether the gears turn or not. Do you have the Pro or Pro-fish model? You have checked that the clutch is tight?
 
On our 2015 R31-cb the bow thruster all of a sudden started spinning with no effect. After watching the appropriate Youtube video and speaking with Imtra customer service, I easily replace the shear pin in less than an hour. The hardest part was removing and bedding and then replacing it at the conclusion. We had Imtra Side-Power SE 40/125S and the shear pin # is SM32050 (old #) or SM32050A (new #) - same part.
 
I didn't notice a thread like this, but on all of the van and vehicle forums I am in there is one like it.

What little fix did you do today that you want to share? Did you reseal a thruhull that was giving you problems? Share the process so someone may benefit.

It's a fun way to show off the cool little things that we all have to do all the time so people can see the day to day stuff! I

We recently purchased a 2022 C-32.
I have had the boat one week. When returned to the dock after short trip both thrusters failed after a few seconds of use. After tiring up, I found warning lights on the generator panel. The only thing in common between the generator and the thrusters is the shared battery. The battery did did even move the needle on the battery display. I spent the next day replacing the thruster battery. I replaced the deep cycle battery, that came with boat, with a Odyssey Dual Purpose battery. I now have plenty of power for the thrusters and the generator.
 
I recently removed the upper helm seat (a stout friend cracked the wood seat bottom) and replace it. It was somewhat easy to create the template and re-wrap the 3/4" marine plywood seat bottom. Also replaced the shear pin in the bow thruster......as easily as I had hoped it would be.
 
While looking for a glycol seepage somewhere around the front of my 2014 D1-30 I noticed that the belt looked to be a little tired. Removed it and could see the fine cracking typical of these type of belts. After 11yrs and 3420hrs it was probably long overdue for a changeout. Hopefully I’m good for another long run with the new one now installed. Never did find the glycol seepage so will continue to monitor I guess.IMG_1892.jpeg
 
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